Hello.
So, here it today's update. There has been some success but also some failures to speak about.
18000
During the week I managed to make another set up top worm gears for the engine. This time I made them as closely to the originals that I could manage. The outside diameter was machined to match the originals plus I also increased the gear tooth depth a little.
I assembled one bogie today to test how they work. What I found out wasn't really what I wanted to happen.
This time, there seemed to be a sticky spot while running. This made the whole thing run unevenly. The weird thing is when I checked the gears on their own, they all seemed to run fine and concentrically. Wen the whole bogie was assembled and running I also noticed there was quite a bit of play on the connection between the bogie and chassis, to the extent the bogie was struggling to stay clipped into the associated housing on the chassis.
Rather annoyingly too, the problems with the mechanism stalling when I twisted the bogie was still there. On top of that, the bogie was binding when I pressed down on it to push it together with the main chassis too.
The top gear was made 1.5mm wide to match the original as I mentioned. I then decided to machine this gear to 1mm wide to see if that made any difference. It did not.
So, I have to rethink things...
1. There is a problem with the connection between the bogie and the chassis. This needs to be reworked somehow as there is far too much play. There is not only some sort of problem vertically, but also too much play moving the bogie left to right (along the length of the chassis), plus the problem with the bogie engaging with the clip on the chassis.
2. I need to revisit the meshing distances of the gears to try and work out what they are tight and binding. They are 0.3 MOD so should be free running.
3. There is still the outstanding issue with the mesh between the worm and the worm "top" gear to address too. The idea of mounting the worm onto the bogie is sounding more appealing by the minute at the moment, although this would mean a serious modification to things.
So, its all a bit of a nightmare right now with this project. Not really what I needed.
Bowden Calbles.
This 'side' project seems to be going a little better.
During the week I got a delivery of a couple of things for this project. Firstly, some 0.35mm diameter piano wire for a suitable mandrel, then secondly some 0.2mm diameter soft brass wire for winding. I was itching to try this out on my machine and they both worked really well with a couple of lengths of spring wound without any hiccups.
Today, I managed to progress these a bit further.
This is my test track that I have been putting together for a while. It needed a way to operate the points remotely but I didn't want to mount anything under the boards. These bowden cables were ideal as they are so small I could feed them under the rails so, I made a loop on one end of some 0.3mm diameter Phosphor Bronze wire and made a small bracket out of Brass tube and sheet which I mounted next to the point. The other end will oneday be mounted to a slide switch attached to the top surface.
It worked surprisingly well and yes, I will insulate the brass spring under the rails eventually.
Sorry about the quality of the photos too.
Julia
